I started to work on that but got sidetracked with family stuff so I will finish getting the dat file uploaded today. The drone was already powered up since then because I was unaware of the availability of this file at the time. Now I know if they happens again not to power it up again until...
yes i understand that, however if you watch the entire video you can see where the drone eventually corrects it self adjusts to my preset altitude and returns to the boat which is a straight line from the end of the curve over the river. Somehow the yaw glitch self corrected, the data is mixed up
I think I am beginning to understand the more I read. So initially everything was fine I had it hovering behind the boat for approximately 9 minutes, I made a last adjustment to line it up with the back of the boat because of a combination of boat sway and Wind drift. For unknown reasons there...
it might not have been exactly straight but it did return to the boat from that location in RTH mode you can see it in the video. 10:21 it looks like it finally goes into RTH mode.
It did eventually go into RTH mode where the yellow arrow is located and returned to the boat where i eventually reclaimed manual control of it. how do i get the DAT file?
The drone was only 25 ft from the boat and well within the range that the wireless controller for the trolling motor operates. That is the only thing i can think of that would have caused any kind of interference with the drone. They both use GPS guided wireless wifi signals to operate. I...
What does poor magnetic enviroment mean? Do you think it is because of the boat being metal? The trolling motor signal is pretty strong and interfere with the radio and can even cause interference in the fish finder as well. It is wireless and uses gps positioning just like the drone does...
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