crashed drone hit retrn home and raised up into trees. One side of upper body was slightly separated, popped it back in. A rear cylinder in back of camera was loose and popped that back in. Forward sensor didn't function recalibrated. The drone flys, seems gutless compared to before and picture...
Yea, I hit go home and as it was starting to land I took it back up without the sensors activated and ran into a tree. Not fast, but it did bounce around in the limbs (evergreen) on the way down.
I bought the replacement plan because I knew as a newbie I would crash...Just didn't want to use it...
I have restarted it two or three times and tried those instructions and it does not get past the first two dots or being in the normal take off position/flat on the surface feet down.
After a while I just repositioned it anyway, nose down and then nose up and then it prompted me to put it on...
I am trying to calibrate my IMU and I have rebooted it two times. I have used half a battery and it has not prompted me to change positions yet. Is this normal. How long should it take to calibrate?
Thanks
This site uses cookies to help personalise content, tailor your experience and to keep you logged in if you register.
By continuing to use this site, you are consenting to our use of cookies.