Here is the sequence of the incident.
1) There was a brief RC disconnection (T=0)
2) RC reconnected (T=10s). Drone was hovering and in P-GPS mode.
3) Between T=10s and T=22s, Drone remain hoovering regardless of the pilot's stick control
4)...
Normally, for a drone in that size, the pilot would hover it 1.2-1.6 meter above the deck and another guy would be half kneeing and catch both legs with two hands. The Pilot would do CSC instead of waiting the drone to perceives as a landing...
I was told that adjusting the boat to meet the descending drone was difficult.
This was not a normal landing. The pilot had no control over the drone and the landing point was unknown (the drone seems to be updating the Home Point at irregular...
yup. the situation is paradoxical...
It is like, I telling you "I am lying"....
So, on one hand, there is the log of "Go Home (RC Disconnected)" and on the other hand the log is still there (as far as I understand, all log are only live...