After a crash the gimbal on my mavic 3 pro was stuck in the back facing position. I went ahead and bought a new gimbal and camera housing and have installed it. I have tried both the in app calibration and the Pyserial calibration. The in app calibration gets stuck at 40% after what appears to be a load limit on the yaw axis. The pyserial calibration (I'm using Pcode WM260) gives me the errors below. Is this something wrong with the gimbal or do we not have the right pcode for the mavic 3 pro at this time?
Error: No response on calibration command JointCoarse request.
Error: No response on calibration command LinearHall request.
Error: No response on calibration command JointCoarse request.
Error: No response on calibration command LinearHall request.