I had deleted Go4 to try to get Litchi to work with the B300 Moverio glasses. Didn't help so I reloaded the Go4. Set some custom parameters at home and then went to fly at a park. I had tripod mode on and was walking down trail, drone stopped and said "max distance" reached, checked beginner mode and it was not set. So, I went back to a safe landing area, picnic table, and while landing the blades hit a tree from the side. I did not take it out of tripod mode, the tree was big. Continued to land, the side sensors were not active and not sure why because tripod button was set. Landed, went over settings, took off with tripod set but M2 behaved as in P or S mode. I had to go into intelligent mode and toggle to get tripod mode to work. Battery drained, replaced battery and same problem. Although it was in tripod mode the M2 behaved as though it was in P or S mode. Toggling intelligent mode in Go4 was only way to solve problem. I had also recently upgraded to 1.02. RTH was set, 15 Sats, plenty of power. I did not get "max distance" error again. Any insight would be appreciated.
I was planning on flying down the Myakka River but confidence in M2 is greatly reduced.
I was planning on flying down the Myakka River but confidence in M2 is greatly reduced.
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