While practicing RTH procedures, I noticed that my Mavic was shaking as it proceeded to the the RTH point. It seemed as though it was had conflicting control inputs. I did this several times and each time this was occurring. The flight plan portion and RTH home logic worked correctly as far as altitudes and flight path considerations. I also noticed that shaking stopped when the Mavic was over its landing point and started the final descent the shaking stopped. Does anybody have any thoughts to as what may be happening?
Thanks,
Jack
Thanks,
Jack