I am new to the Litchi app and did a few close in test with no issues.
I decided to expand my route out about 1/4 of a mile (still within range of controller) and had a flight plan with 11 waypoints. All close enough to have a full signal.
On waypoint #2... the Mavic just stopped and hovered. I gave it about 30 seconds before I cancelled the trip and took control to bring it back. I am not sure how long it would have stayed there.
I looked at that waypoint and there was nothing special about it. No actions.. cruise speed as default with was 15 mph... I also made sure I did not pause the flight plan.
Does anyone have any ideas on what would cause this? I deleted that way point and reran it with no issues.
I am concerned that if I create a flight plan that may result in loss of signal that I could lose the Mavic since it would not complete the plan and return.
Thoughts?
Thanks,
George
I decided to expand my route out about 1/4 of a mile (still within range of controller) and had a flight plan with 11 waypoints. All close enough to have a full signal.
On waypoint #2... the Mavic just stopped and hovered. I gave it about 30 seconds before I cancelled the trip and took control to bring it back. I am not sure how long it would have stayed there.
I looked at that waypoint and there was nothing special about it. No actions.. cruise speed as default with was 15 mph... I also made sure I did not pause the flight plan.
Does anyone have any ideas on what would cause this? I deleted that way point and reran it with no issues.
I am concerned that if I create a flight plan that may result in loss of signal that I could lose the Mavic since it would not complete the plan and return.
Thoughts?
Thanks,
George