Maiden flight(actually the second time it was in the air, first time was 10 feet high and 4 feet in front of me just to test functions) everything was looking good, great battery management, decent bat% on the turn around, then this happened
Lost satalites, atti kicked in, no problem, but then had no Google map, thank goodness it was daylight, then the camera start panning slowly from one side to the other, it was really disorientating, I did my best to stay on track to the nearest field. Somethings messed up with this bird. Too bad because I would've had plenty of battery. Stock a/c & r/c .400fw
Airdata UAV - Flight Data Analysis for Drones